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Showing posts from September, 2022

Nylon Brake Lines

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During the built of N333ST we decided to upgrade the standard brakes to Matco brakes. I am not entirely sure why we decided to do this, but I think we believed that these brakes would provide superior braking power. In hindsight I now realize that the plane has plenty of stopping power using the standard brakes. Anyway, trouble started during flight testing. After 10 hours or so we noticed a brake fluid leaking from one of the brakes. A friendly mechanic fixed the leak by tightening the fittings that connect the nylon brake lines to the caliper. Unfortunately, the problem came back after we finished flight testing and had flown home. We assumed (incorrectly) that the nylon line was not fitted properly into the caliper, and the bent was causing a leak. To fix this I ordered a bunch of brake line parts online and tried to install a contraption to better line up the brake line with the fitting. Each time, this required bleeding the brakes, which in itself is a pain in the rear. Long stor

Floor under Back Seat

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For some strange reason, there is no floor under the back seat. I guess Sling expects the back seat to cover any cold air leaks and stop stuff from falling into the space below. This seems really sub-optimal, dangerous, and needs to be addressed. Without a floor, the seat belt buckles can be pushed through the seat and fall into the space below which houses many important linkages that are needed to fly the plane, so that could be bad. Also there is a huge amount of cold air leaking into the cabin from underneath the seat. To fix this I decided to add aluminum floor panels under the rear seats, to close up the space. They are mounted with rivnuts, covered in carpet, and easily removed for inspection. The final result shown in the first picture.  It is an easy build; you need a rivnut tool, metal scissors , rubber mallet, and a few others. Measuring, fitting, and installing requires various advanced yoga poses, but it is doable. First I made a cardboard template for the two panels, meas

Prop Controller Failure

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 On our way back from Oshkosh we experienced a prop controller failure. Three blinking red lights, which according to the documentation  indicates "Slipring Brush Worn Out". This had to happen at the worst possible time just as we were arriving at Wendover airport ( KENV ) which is at an altitude of 4200 feet and was reporting 45C.  I can't remember the exact density altitude, but it was definitely greater than 8000 feet. Luckily we had some intermittent manual control and we were able to get the prop into a position where we could continue to fly, keeping a close eye on the engine RPM, making sure not to overspeed it.  After refueling we departed using RW08 (10000'), and we were able gain altitude without any trouble. But during the climb out, to add insult to injury, the GTN650 decided to overheat and report a "Cooling Fan Failure". Luckily that cleared up as we got into higher and (slightly) colder air. Back in KPAO I emailed  Airmaster  in New Zealand. W

External Static Air Intake

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When we finished the build of N333ST, the static air intake was located behind the panel. This has been so for all Slings built so far. However, as we have fixed some cabin air leaks the internal pressure has changed and the airspeed is now clearly reading too high by perhaps 20 knots. That is not a good situation.  So this week I returned to TAF in Torrance to install the newly released External Static Air intake kit. The kit consists of two external ports, some tubing, an intake switch that is mounted in the instrument panel, and some instructions. We were the first to install the kit. Shawn completed the installation in a few hours, and that same afternoon I performed a quick test flight with Jean. The airspeed was much more consistent, and noticeably lower than before.  However, the switch was not installed correctly. Switching to internal static air caused the airspeed to quickly drop. Jean quickly analyzed the problem, and the next day we hooked up the switch correctly. Now it wo